New Build Needing Firmware Help!
Posted: Fri Oct 18, 2013 2:56 pm
Hello everyone!
I've just finished getting my Rostock Max built.
I was able to connect it to Repetier Host (.90c) and I even uploaded the latest github Rostock Max firmware via Arduino IDE.
My trouble is this...certain commands to the motors don't seem to be responding properly.
The most obvious example is when I try to call G28. All of the motors move up towards the home switches as they should, but they stop moving after only maybe an inch or so of upward movement. If I send another G28 code, they will once again move up towards the home switch but again stop after about an inch or so of movement. Weird.
Using the manual controls in RP I am pretty sure I was able to move each of the three axis (can't remember if I moved all three manually but definitely at least two) although it seemed to be with the same sort of single short movements.
What could be the culprit in a situation like this?
I read something online somewhere about perhaps the units being incorrect when travel is shorter than it should be, but I would assume the units are right since the firmware was flashed directly from the latest on the SeeMeCNC website??
It may also be worth noting, this kit was ordered I think in April. I recall there are a different number of steps on some of the Rostocks?
Anyway, all help is immensely appreciated.
Thanks in advance!
-Daniel
Portland, Oregon
I've just finished getting my Rostock Max built.
I was able to connect it to Repetier Host (.90c) and I even uploaded the latest github Rostock Max firmware via Arduino IDE.
My trouble is this...certain commands to the motors don't seem to be responding properly.
The most obvious example is when I try to call G28. All of the motors move up towards the home switches as they should, but they stop moving after only maybe an inch or so of upward movement. If I send another G28 code, they will once again move up towards the home switch but again stop after about an inch or so of movement. Weird.
Using the manual controls in RP I am pretty sure I was able to move each of the three axis (can't remember if I moved all three manually but definitely at least two) although it seemed to be with the same sort of single short movements.
What could be the culprit in a situation like this?
I read something online somewhere about perhaps the units being incorrect when travel is shorter than it should be, but I would assume the units are right since the firmware was flashed directly from the latest on the SeeMeCNC website??
It may also be worth noting, this kit was ordered I think in April. I recall there are a different number of steps on some of the Rostocks?
Anyway, all help is immensely appreciated.
Thanks in advance!
-Daniel
Portland, Oregon