G29 issues after conversion to HE280
Posted: Mon Mar 06, 2017 4:14 am
I have upgraded my V2 machine for the HE280.I have previously upgrades the following;
Cheap Skates
Arms
power supply
I have had the issues that other people seem to have The accelerator system did not have a proper ground, I have it wired right now and I am continuing the calibration process starting with G29... Head comes down close to the bed the moves toward the left front tower then moves down and crashes and continues to move off the the glass and off the plate. I have to kill the power. Her is the terminal ourtput before I kiil the printer
"
->G29
<-ok
<-
<-TargetExtr0:0
<-
->M114
<-Transformation matrix: 1.000000 0.000000 0.000000 0.000000 1.000000 0.000000 0.000000 0.000000 1.000000
<-
<-SpeedMultiply:100
<-
<-X:0.00 Y:0.00 Z:365.738 E:0.0000
<-
->M105
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-Z-probe state:L
<-
<-zprobing...
<-
->M105
"
I have checked the PW-ON lead and it looks OK... But I get the impression that the interrupt is not happening.
Any Ideas?
Cheap Skates
Arms
power supply
I have had the issues that other people seem to have The accelerator system did not have a proper ground, I have it wired right now and I am continuing the calibration process starting with G29... Head comes down close to the bed the moves toward the left front tower then moves down and crashes and continues to move off the the glass and off the plate. I have to kill the power. Her is the terminal ourtput before I kiil the printer
"
->G29
<-ok
<-
<-TargetExtr0:0
<-
->M114
<-Transformation matrix: 1.000000 0.000000 0.000000 0.000000 1.000000 0.000000 0.000000 0.000000 1.000000
<-
<-SpeedMultiply:100
<-
<-X:0.00 Y:0.00 Z:365.738 E:0.0000
<-
->M105
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-accelerometer send i2c error.
<-
<-accelerometer i2c recv error.
<-
<-Z-probe state:L
<-
<-zprobing...
<-
->M105
"
I have checked the PW-ON lead and it looks OK... But I get the impression that the interrupt is not happening.
Any Ideas?