Overhauled my EZstruder :shock:
Posted: Tue Sep 02, 2014 5:55 pm
Guys, I have a confession to make: I modded my EZstruder. I modded it like woah.
There have been two ongoing issues with my RMax, first that I haven't been able to print PLA reliably since switching to an E3D v5, and also my ezstruder would occasionally kickback, even with ABS. It was much, much worse with PLA. Recently I replaced the E3D with the new Prometheus, and while it handled PLA much better, the poor extruder still choked occasionally. After putting a heatsink on the stepper driver and a fan on the extruder motor without any effect, I decided to change things up.
The hobbed gear on the extruder is a MK7 (or similar), which has an effective diameter of ~10mm. I bought a MK8, which has an effective diameter of ~7mm, which should therefore yield about 30% more torque, while not limiting my retraction speed nearly as much as a planetary geared motor would. The trouble is that with the smaller diameter, the filament would then run much closer to the motor shaft, so all of the channels in the ezstruder would be misaligned. I tried it, it didn't work. Soo...I did a major redesign on the extruder.
[img]http://i61.tinypic.com/nxownp.jpg[/img]
The upper section was altered so the platform the spring rests in is higher, putting more force on the red arm. The clear plastic cover was replaced with a simple rectangle that serves the same purpose of keeping the spring and arm secure. Most of the overhaul is in the lower section. Everything was moved more towards the center to align better with the filament. The metal groovemount cylinder that the pushfit connecter screws into was replaced with one that has threads for an E3D style passthrough connector, which I printed on my DLP resin printer. This allows the bowden tube to run straight up to the hobbed gear, so the filament is only unsupported there for a few mm. The passthrough connector stops the tube from going down, but retraction made it start creeping up into the gear, so I wrapped some kapton tape around the tube to keep it firmly in place. The other main change was making the whole thing thicker, so I could flip the hobbed gear to have the grub screw closer to the motor and out of the way of the red arm. This meant I had to cut away one side of the top piece so the grub screw is still accessible.
I've just started my first test print with it, which has been running for only about 30 minutes now, but so far there hasn't been any kickback, no sudden *THUNK* sounds, and the PLA seems to be laying down nice and smooth. If anyone wants the files to try this design, I'd be happy to post them. You'll just need a MK8 hobbed gear, a passthrough pushfit, and a couple new screws...I should've made a note of what I was using, but didn't. XD
There have been two ongoing issues with my RMax, first that I haven't been able to print PLA reliably since switching to an E3D v5, and also my ezstruder would occasionally kickback, even with ABS. It was much, much worse with PLA. Recently I replaced the E3D with the new Prometheus, and while it handled PLA much better, the poor extruder still choked occasionally. After putting a heatsink on the stepper driver and a fan on the extruder motor without any effect, I decided to change things up.
The hobbed gear on the extruder is a MK7 (or similar), which has an effective diameter of ~10mm. I bought a MK8, which has an effective diameter of ~7mm, which should therefore yield about 30% more torque, while not limiting my retraction speed nearly as much as a planetary geared motor would. The trouble is that with the smaller diameter, the filament would then run much closer to the motor shaft, so all of the channels in the ezstruder would be misaligned. I tried it, it didn't work. Soo...I did a major redesign on the extruder.
[img]http://i61.tinypic.com/nxownp.jpg[/img]
The upper section was altered so the platform the spring rests in is higher, putting more force on the red arm. The clear plastic cover was replaced with a simple rectangle that serves the same purpose of keeping the spring and arm secure. Most of the overhaul is in the lower section. Everything was moved more towards the center to align better with the filament. The metal groovemount cylinder that the pushfit connecter screws into was replaced with one that has threads for an E3D style passthrough connector, which I printed on my DLP resin printer. This allows the bowden tube to run straight up to the hobbed gear, so the filament is only unsupported there for a few mm. The passthrough connector stops the tube from going down, but retraction made it start creeping up into the gear, so I wrapped some kapton tape around the tube to keep it firmly in place. The other main change was making the whole thing thicker, so I could flip the hobbed gear to have the grub screw closer to the motor and out of the way of the red arm. This meant I had to cut away one side of the top piece so the grub screw is still accessible.
I've just started my first test print with it, which has been running for only about 30 minutes now, but so far there hasn't been any kickback, no sudden *THUNK* sounds, and the PLA seems to be laying down nice and smooth. If anyone wants the files to try this design, I'd be happy to post them. You'll just need a MK8 hobbed gear, a passthrough pushfit, and a couple new screws...I should've made a note of what I was using, but didn't. XD