G28 z-axis on RAMBo not responding?
Posted: Tue Aug 13, 2013 12:28 am
First off i did a search on "G28" and i couldn't find anyone with my exact problem I'm experiencing.
Just got the Rostock Max assembled and starting doing ch 17 in the ver2 pdf
I configured my Repetier as closely to the books as possible, I am running ver 0.90c and the "connection" tab under printer settings is a little bit different
I get to the part where you enter g28, the x and y started going down and the z remained still.
I found and made true the inverse parts in "configuration.h", ran g28 again the x and y are now going up but the z still remains still
I swap x and z connection on the board, run g28 again and z and y go up and x remains still
Although my servos shipped with the connectors installed a checked, and with that switch test i performed it proves that the connectors themselves aren't the problem
I return the connectors back to the correct location on the board, and try to move z in "manual control" tab, i just get a bunch of humming and no motion.
I imagine i could test the second z motor port on the board but i am unsure where to configure that.
Thanks for the input in advance
Just got the Rostock Max assembled and starting doing ch 17 in the ver2 pdf
I configured my Repetier as closely to the books as possible, I am running ver 0.90c and the "connection" tab under printer settings is a little bit different
I get to the part where you enter g28, the x and y started going down and the z remained still.
I found and made true the inverse parts in "configuration.h", ran g28 again the x and y are now going up but the z still remains still
I swap x and z connection on the board, run g28 again and z and y go up and x remains still
Although my servos shipped with the connectors installed a checked, and with that switch test i performed it proves that the connectors themselves aren't the problem
I return the connectors back to the correct location on the board, and try to move z in "manual control" tab, i just get a bunch of humming and no motion.
I imagine i could test the second z motor port on the board but i am unsure where to configure that.
Thanks for the input in advance